Stock carb. I’ve tried 38, 40, and 42 pilot jets all with no effect on idle. I cleaned the carb very well and installed a fresh rebuild kit with brand new Keihin jets. The choke lever has been removed. (and plugged) Accelerator pump works perfect and bike starts easy cold or hot. (As long as I give it a few squirts)
K&N filter with holes drilled in lid, snorkel tube plugged off
Fresh 440 kit from Niche Industries (Ebay) advertised 10:1 ratio. This piston is flat top I’m not sure if it’s actually 10:1. it seems to be 9:1. Compression test shows 120 psi so either it’s low or not 10:1. I haven’t been able to give it a proper break as I have yet to get the carb tuned because of this idle issue.
Fresh head from Niche as well. Used valves.
Here’s the other strange issue I’ve having. I noticed when it is running, it has a slight oil leak from the head cover gasket towards the exhaust side, just above the header. After shutting it off and cleaning the oil and letting it sit over night, I came back in the morning to find that it continues to leak very slowly while not running. When running however, it leaks faster and I can even see very small bubbles coming through the oil. Not sure if there’s compression blow-by pressurizing case. The gasket must be bad, although it looked to be in perfect shape and I used a spray on copper based gasket sealant.
Anyway, thanks for reading and thanks for any tips or thoughts on the carb issue. I took the carb off and I’m going through it one more time to make sure everything is clean! I’m stumped!